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gu patrol lacking power and hard to start

Posted: Fri Nov 27, 2009 11:59 am
by jarchiemarchie
i have 1999 gu 4.2td and i recently changed my fuel filter which had rust on the top of it and within bout 20 mins of it my car was lacking power and cuts out at bout 3500 rpm in 2nd gear if you get up it is there any filters between the main filter and the injectors i have had my turbo checked out and its fine and dont have egt guage so i cant tell what its running on

Posted: Fri Nov 27, 2009 3:21 pm
by tna racing
bleed it up properlly?

Posted: Fri Nov 27, 2009 5:08 pm
by Look'n 4 Mud
Yep. sounds like it is sucking air.

I have an aftermarket with a glass bowl and water separator. You can see it "drip" air into the system if it is not tight enough.

Tight enough can be pretty bloody tight mate.

Bleeding can be a bitch, try tightening it first and taking it for a spin if no joy start cracking injectors and bleeding out.

Good luck.

Posted: Wed Dec 02, 2009 9:35 pm
by Tomo_89
there is a thimble filter under the banjo fitting on the supply line to the pump. this can get clogged up and give poor power

Posted: Thu Dec 03, 2009 3:06 pm
by gu town
Tomo_89 wrote:there is a thimble filter under the banjo fitting on the supply line to the pump. this can get clogged up and give poor power
x2

try that little filter first before cracking injectors. some people just throw it out. i did 2 years ago and still going strong. but each to their own.

undo banjo fitting.

there'll be a spring down in the hole you pull the bolt out of, remove that.

then there'll be a little brass looking gauze thimble filter you might not be able to see through the diesel


you might need a fine bit of wire bent in the shape of a tent peg to hook it out.

hope it helps. i thought i was up for an injector pump before i did this.

try these for a few pics.
http://www.outerlimits4x4.com/ftopic760 ... ble+filter
http://www.outerlimits4x4.com/ftopic153203.php

Posted: Sat Dec 12, 2009 1:12 pm
by jarchiemarchie
hey cheers for the help it was the little filter in the banjo fitting it was full of crap and now i have cleaned it and put it back its running consierably better