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lost some boost TD42T
lost some boost TD42T
had my GU ute out at cruiser park over the last 5 days and have given it the best (and also roughest) drive since i have had it. on the way home though i noticed i had lost 3lbs boost.
i havent touched the motor since i bought it but installed an autometer boost gauge which gave me a reading of 14psi under heavy load. now its flatout trying to get 12.
i noticed a small loss in power (especially when boost comes on, of course) so i'm sure it cant be a gauge problem. could the boost controller (i think thats what it is) have adjusted with the rough driving? i cant seem to see any leaks anywhere either.
any other thoughts????
thanks
PAUL
i havent touched the motor since i bought it but installed an autometer boost gauge which gave me a reading of 14psi under heavy load. now its flatout trying to get 12.
i noticed a small loss in power (especially when boost comes on, of course) so i'm sure it cant be a gauge problem. could the boost controller (i think thats what it is) have adjusted with the rough driving? i cant seem to see any leaks anywhere either.
any other thoughts????
thanks
PAUL
Check trips and Tracks sectionvoidroid wrote:Why is there no pics, discussion regarding Landcruiser Park Mud Bulls? Have I missed a completely different forum for posting information on this event because otherwise I would assume no one was interested in that event? Confused...
GU 4.2 TD Garrett BB Hi-flow, M8274 + Bells & Whistles with plenty of fruit still on the list!
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[b][color=red]\ m / ( > . < ) \ m /[/color][/b]
cleaned the air filter this morning and managed to bounce off 13psi boost giving it hard. but i dont get the spooling that i used to. it just doesnt accelerate as quickly. im still looking to find an extra 1psi or so as well. fuel filter will be the next thing to do.
do wastegates sh*t themselves?
PAUL
do wastegates sh*t themselves?
PAUL
Road Ranger
its always in the last place you look dude
what air filter? maybe replace the filter?? when mine lost all boost it turned out there was a crack in the air box which let some mud and crap in and totally cloged the filter up, I cleaned it right out which helped but it wasnt right until I replaced the filter....factory paper set up
what air filter? maybe replace the filter?? when mine lost all boost it turned out there was a crack in the air box which let some mud and crap in and totally cloged the filter up, I cleaned it right out which helped but it wasnt right until I replaced the filter....factory paper set up
If the above post did not offend you in any way please PM me so I can try harder!!
i'm sure its not an air problem anymore. have a k&n air filter (oily) and yes it was clogged...but cleaned it several times. even went for a short drive without air filter element and no difference. will prob end up going back to paper filters as oil ones turn dust into mud.
im able to get what my gauge reads as 13psi now...but still not getting the kick in the ass that is spooling. it doesnt feel like it "comes on boost" like it did.
bogged is right...ill do a couple more "at home" tests and order a 3in dump pipe, fit that up along with pyro and send it in for a tune....
PAUL
im able to get what my gauge reads as 13psi now...but still not getting the kick in the ass that is spooling. it doesnt feel like it "comes on boost" like it did.
bogged is right...ill do a couple more "at home" tests and order a 3in dump pipe, fit that up along with pyro and send it in for a tune....
PAUL
unlikely but possible.
some of the 4.2 turbo diesels have a blow off valve as well as the wastegate (not sure about the 3.0's)
go to a plumbing supply store and get a 1" BSP copper plug (male thread) unscrew the blow off valve and put in the plug. The spring weakens over time and lets boost out earlier and earlier. some crud could have got caught in it. if this isn't the cause it's worth doing anyway.
Matt
some of the 4.2 turbo diesels have a blow off valve as well as the wastegate (not sure about the 3.0's)
go to a plumbing supply store and get a 1" BSP copper plug (male thread) unscrew the blow off valve and put in the plug. The spring weakens over time and lets boost out earlier and earlier. some crud could have got caught in it. if this isn't the cause it's worth doing anyway.
Matt
2000 GU ST Patrol 4.2 turbo oiler not so bog stock anymore
"EVILGU"
"EVILGU"
It sounds like a boost leak. I had the same thing when i had a turbo subaru. it didnt seem to come on boost as hard. Kinda felt really doey or like it had really bad turbo lag. I had a boost leak on one of the intercooler manifold's. The reason it doesnt seem to pull like it used to even though you have only lost 1psi is due to a lack of volume.
just put a new fuel filter on. it had about 6-8mm of sludge in the bottom of the old filter. but unfortunately made no difference.
ordered a 3in dump pipe today and when it is installed will get the chance to have a squiz at the wastegate. then it will be off for tune. ill notify them of the problem and hopefully resolve it
PAUL
ordered a 3in dump pipe today and when it is installed will get the chance to have a squiz at the wastegate. then it will be off for tune. ill notify them of the problem and hopefully resolve it
PAUL
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