Notice: We request that you don't just set up a new account at this time if you are a previous user.
If you used to be one of our moderators, please feel free to reach out to Chris via the facebook Outerlimits4x4 group and he will get you set back up with access should he need you.
Recovery:If you cannot access your old email address and don't remember your password, please click here to log a change of email address so you can do a password reset.

gq 4.2 turbo (low boost dont know why??)

Tech Talk for Nissan owners.

Moderators: toaddog, V8Patrol

Post Reply
Posts: 8
Joined: Thu Dec 10, 2009 4:50 pm
Location: traralgon

gq 4.2 turbo (low boost dont know why??)

Post by lippy4x4 »

I am trying to wind the boost up on my gq and it can only spool up to 14(dts setup). I have tried adjusting the rod on the actuator and it is out of adjustment. I have a boost adjuster on and it is out of adjustment, also I have tried to block the actuator off so it gets no presure to trip the wastegate valve. The valve moves freely and sounds like it hits metal when you open and close it.

What could i do to try get more boost out of this turbo.
Posts: 345
Joined: Wed Dec 24, 2008 11:58 am
Location: Mackay

Post by tye1986 »

maybe needs more fuel...
gq coil cab with stuff
Posts: 248
Joined: Fri Jan 16, 2009 12:48 pm
Location: Sth Wst QLD

Post by 300WinMag »

You need to increase the preload pressure on the actuator as the exhaust pressure will push the wastegate poppet valve open. I had to weld mine shut to get up to 20 psi out of it but my turbo is high flowed and modified.
And yes I have bigger pump and injectors plus custom water to air intercooler.
Last edited by 300WinMag on Wed Feb 17, 2010 5:30 pm, edited 1 time in total.
Posts: 41
Joined: Fri Jul 24, 2009 1:22 pm
Location: Wodonga Vic

Post by BOOSTED GQ »

tye1986 wrote:maybe needs more fuel...
x2 you need more fuel. Mine could only make 14 pound when Igot it with the actuater line off screwed the pump up ond off she went.

If you dont have one get a pyro gauge
Posts: 388
Joined: Wed May 14, 2008 6:01 pm
Location: the sticks gippsland

Post by waandy »

my utes gona kick ur shortys arse lippy ha ha pyro it and fuel it up, rohs dts kit runs 14 15 psi without even adjusting it man, he just bolted it strait on
85 hi top drover, 31s, 2 inch exended shackles 2 inch bl.
88 tb42 swb mav,35 claws, 4 inch lift
Posts: 8
Joined: Thu Dec 10, 2009 4:50 pm
Location: traralgon

Post by lippy4x4 »

thanks fellas, the other day i adjusted the fuel 1/8 of a turn and it made a little difference but not much. i have a pyro and the etg is up aroung 400. i didnt want to put more fuel in if it wasnt going to change the boost presure.
Posts: 1350
Joined: Tue Nov 25, 2008 4:48 pm
Location: Sunshine Coast - Brisbane

Post by money_killer »

lippy4x4 wrote:thanks fellas, the other day i adjusted the fuel 1/8 of a turn and it made a little difference but not much. i have a pyro and the etg is up aroung 400. i didnt want to put more fuel in if it wasnt going to change the boost presure.
just get it dyno tuned ur just wasting ur time
94 Patrol Petrol 3.0L lift, tyres, winch
90 WT Serria locked diff, Muddies
Posts: 8
Joined: Thu Dec 10, 2009 4:50 pm
Location: traralgon

Post by lippy4x4 »

how much boost should a dts turbo put out? Would it be much more than 14psi?
Posts: 1040
Joined: Fri Jun 29, 2007 7:57 pm
Location: yatala, halfway between brisbane and GC

Post by love ke70 »

if its maxing at 400 degrees your pyro is either reading wrong or you have a whole heap of headroom to add fuel, which will make more boost
97 GQ patrol coilcab. TD42, safari turbo kit with fiddled turbo, D-GAS kit. dyno results to come...
4inch lift, king springs, efs and procomp shocks
315/70R16 cooper ST's
found fuel economy...
Posts: 257
Joined: Sun Mar 25, 2007 7:44 pm
Location: D' Aguilar

Post by beast of a GQ »

I always thought you could comfortably goto around the 600 mark. Correct me if im wrong. And i no a few guys go further than that again.
04 GU Wagon 3L TD. 33's, 3" flexy coil lift. Kicker stereo, LOUD

GQ TD4.2 Extra Cab, 6" Flexy coil lift, Pro comps, 3rd's upper and lowers, 37 boggers. Plenty more to come.
Posts: 1040
Joined: Fri Jun 29, 2007 7:57 pm
Location: yatala, halfway between brisbane and GC

Post by love ke70 »

recommended lift point is 550* post turbo

depends how good your pyro is though...
97 GQ patrol coilcab. TD42, safari turbo kit with fiddled turbo, D-GAS kit. dyno results to come...
4inch lift, king springs, efs and procomp shocks
315/70R16 cooper ST's
found fuel economy...
Posts: 4275
Joined: Thu Dec 19, 2002 2:12 pm
Location: Sydney

Post by ozy1 »

i had the dts kit on my gq, i bloked the waste gate actuator line, and it hit the stopper on my boost guage, it was only a 20psi guage,
Posts: 612
Joined: Mon Nov 20, 2006 9:32 pm
Location: sunny coast

Post by shw337 »

i just had my pump built, and when we re-installed it i cud winde the boost adjuster right out and it quite freely goes over 25psi so i set it at 20. egts get to 500 quite easly but back off and they drop away just as quick. on a hiflo denco kit with water to air and $$$$ pump
89 4.2tdt pootrol,w-a,3inch spring,bar-reparing,83%ers,4.6, arb front & noslip rear, 35's
tree mended guards
Posts: 8
Joined: Thu Dec 10, 2009 4:50 pm
Location: traralgon

Post by lippy4x4 »

shw337 wrote:i just had my pump built, and when we re-installed it i cud winde the boost adjuster right out and it quite freely goes over 25psi so i set it at 20. egts get to 500 quite easly but back off and they drop away just as quick. on a hiflo denco kit with water to air and $$$$ pump
I just turned the fuel up and it doesnt get anymore than 14psi boost. does this sound like the turbo is nackered or what could it sound like??
Posts: 345
Joined: Wed Dec 24, 2008 11:58 am
Location: Mackay

Post by tye1986 »

maybe be a crack in the rear housing where the waste gate seals...
gq coil cab with stuff
Posts: 252
Joined: Fri Sep 02, 2005 3:45 pm
Location: outside your window

Post by hiy6o »

What about a blocked exhaust ? happened on my turbo petrol would not make high boost even though it still went ok dropped the dump pipe off and it maxed out my boost guage and blew an intercooler hose off .
Nup not telling
you'll have to find out yourself
Post Reply

Who is online

Users browsing this forum: No registered users and 25 guests