![Image](http://i78.photobucket.com/albums/j101/Mr_DJ_photos/Ford%20conversion/head%20gasket%2014-5-12/IMAG0203.jpg)
Wynnum Engine Reconditioners tested them and found no cracks but needed 8 thou to face them (previous gasket marks could still just be seen in a couple places) and a valve grind while out to ensure excelent valve sealing seemed smart while they were out.
Had to buy a set of ARP head bolts ($60) as they were not used as promised in the initial rebuild
![cussing :bad-words:](./images/smilies/new_cussing.gif)
![Image](http://i78.photobucket.com/albums/j101/Mr_DJ_photos/Ford%20conversion/head%20gasket%2014-5-12/IMAG0213.jpg)
Fel-Pro VRS gasket set was used (nice kit) and at 2:30am Friday morning it was almost back together.
![Image](http://i78.photobucket.com/albums/j101/Mr_DJ_photos/Ford%20conversion/head%20gasket%2014-5-12/IMAG0220.jpg)
Had to get a few little things when the sun came up, idler pulley bearing was bit sad & broke a couple of injector locking clips in my rush to pull the heads off on monday night to get them to the machinist.
All back together and started straight away :peaceout: I thought all is great, so changed the oil & filter, bleed the cooling system, loaded the rig & trailer and set off for The Hilux Meet around 4:30pm.
Just after getting on the highway (not far from home) the temp climbed to 100deg so cruised back home to sort the problem which I thought to be a thermostat as it was holding 100deg all the way back.
Pulled the thermostat, tested it in water on the stove and was open before it reached a simmer so that was not the problem.
All back together again, bleed it for 2hrs + a short run up the street and STILL getting some very fine air bubbles out the rad.
Thinking it's an air lock somewhere but otherwise I just about out of ideas.
Short vid below.
![Image](http://i78.photobucket.com/albums/j101/Mr_DJ_photos/Ford%20conversion/head%20gasket%2014-5-12/th_VIDEO0014.jpg)